Climate
Change & Environmental Services (CCES) managed the construction
management and environmental permitting for a major boiler modernization
project for a large apartment complex in New York City that has reduced
emissions and saved the complex over $2.8 million in fuel costs compared to the
previous 12-month period.
East River Housing (ERH) Corporation operates a boiler house
providing heat and hot water to a number of apartment buildings with over 2,700
units plus a shopping center. It had been combusting over 2 million gallons of
No. 6 fuel oil annually. The housing corporation decided to modernize the
boilers and switch from fuel oil to natural gas.
ERH replaced one aging boiler with a new modern unit and
renovated its other two existing boilers, installing new low NOx burners with
flue gas recirculation. ERH worked with Con Edison, the local utility, to bring
a natural gas line into the boiler house for the fuel switch.
No. 2 diesel oil is to be used as a backup during natural
gas interruptions, necessitating the installation of a new tank farm replacing
the No. 6 fuel oil tank farm.
CCES carried out construction management to address
scheduling and technical issues with the implementation of the installation and
testing, as well as all environmental permitting. The physical installations
are complete and the plant has operated under natural gas for one full year
now.
CCES has assessed the cost savings due to the project. Given
natural gas being piped to the facility, removal of No. 6 oil tanks, and use of
a modern No. 2 oil tank farm, ERH virtually eliminated the risk of a messy oil
spill in the densely populated area. In addition, emissions of pollutants
critical in an urban area all markedly dropped because of this project, such as
NOx (85%), particulate matter (75%), greenhouse gases (equivalent of removing
4,600 cars from the road), and SO2 (99%). These reductions helped change the
permitting status of ERH from major to minor, saving them much in fees and
removing several regulatory requirements.
CCES determined that themal efficiency improved by about 18%
(fewer therms to create steam). “We are not sure if the thermal efficiency
improved because of natural gas being more fluid than No. 6 fuel oil, which is
thick and viscous or because of the new equipment. But probably both
contributed,” said Marc Karell, principal with CCES.
CCES also calculated cost savings. In the 12 months of
natural gas service (May 2012 through April 2013), ERH directly saved over $2.8
million (63%) in fuel costs compared to the previous 12-month period, despite
this being a measurably colder winter than the one before. CCES also calculated
avoided cost savings (added fuel costs ERH would have had to incur if ERH still
combusted No. 6 fuel oil with the old boilers).
The avoided cost savings for the 12-month period was conservatively estimated
to be over $5.3 million.
The project payback, initially anticipated to be about 4
years, will be under 2.5 years based on direct cost savings.
Asked if switching from fuel oil to natural gas was a viable
option for other facilities, Karell said it depends on the availability of
natural gas and the cost of extending a natural gas line to the site.
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